Refine Your Search

Topic

Author

Affiliation

Search Results

Technical Paper

Recovery of Selected Engineering Plastics from Automotive Shredder Residue Using Skin Flotation Technology

1999-03-01
1999-01-0663
Recovery of metals from automobile shredder residue (ASR) is currently being applied to over 11 million end of life vehicles (ELV) in North America. However, most plastics from these vehicles become landfill. The Vehicle Recycling Partnership (VRP), an effort of Chrysler, Ford, and General Motors, as part of the USCAR initiative, has been conducting research to recover plastics from this ASR feed stream. The VRP has been working with Recovery Plastics International (RPI), to investigate automated plastic separations. RPI has been developing processes that would allow for fully automated recovery of target engineering plastics. The portion of the process developed for separating the engineering plastics is called skin flotation. This technology can separate engineering plastics even if the materials have the exact same density. A pilot production line has been set up for processing a variety of commercial ASR materials at RPI in Salt Lake City, Utah (USA).
Technical Paper

Aeroacoustics of an Automobile A-Pillar Rain Gutter: Computational and Experimental Study

1999-03-01
1999-01-1128
Noise due to the flow over an automobile A-pillar rain gutter in isolation was computed using a two step procedure. Initially the flow solution was obtained by solving the Reynolds Averaged Navier Stokes (RANS) equations. Acoustical Sources were extracted from the flow solution and propagated to the far-field using the Lighthill-Curle equation. Experiments were conducted to evaluate the computations. Compared results include steady pressures, time dependent pressures, and sound intensity levels. Computed results and experimental data were reduced in a similar way to ensure a one to one comparison. Computed results are in good agreement with the experimental values. A-weighted noise levels are predicted reasonably well.
Technical Paper

Automobile Exterior Water Flow Analysis Using CFD and Wind Tunnel Visualization

1998-02-23
980035
This paper presents an innovative automobile application of Computational Fluid Dynamics (CFD) as a complement to wind tunnel experimentation for the evaluation of rain water and wiper wash flow on the exterior of a moving vehicle. In addition to calculating the air flow around a car, a multi-phase CFD code was used to simulate rain drops in the air stream, rain drops impinging on the vehicle, and the transport of the “thin liquid film” of water on the vehicle surfaces. Time-dependent results for the location, velocity, and height of the water film on the windshield, A-pillar, and side glass were obtained. The CFD results compared favorably with a wind tunnel procedure. The variation of the calculated water film corresponded with observed patterns of water streaks on test vehicles. Design iterations performed on the computational model also agreed with similar test configurations.
Technical Paper

Design of a Dual Wall Air Gap Exhaust Manifold

1998-02-23
980045
The new regulations to reduce emissions have resulted in the development of new techniques to maintain or enhance competitive performance. A requirement for the manifold is to help meet the reduction in cold start emissions, particularly during the transient conditions from start to 100 seconds following the Federal Test Procedures for vehicle emissions. Finite element computer models were developed to predict inner and outer wall temperatures, and to determine structural soundness. Tests were performed to assure that noise levels were minimized. Dynamometer lab and field tests were performed to verify that the manifold would meet the design requirements. From the results of these tests and analyses, modifications were made to the weld and manufacturing techniques to improve product life and reduce noise. Dual wall manifolds have proven durability to meet high exhaust gas temperatures up to 1650°F (900°C), while meeting the performance, noise, and weight reduction goals.
Technical Paper

Accelerated Glass Reveal Molding Test

1998-02-23
980718
Over the past 20 years, polyvinyl chloride (PVC) has almost replaced metal in stationary glass reveal moldings with dramatic part cost savings on cars and trucks world-wide. The process of assembly is generally simple and convenient but to replace a reveal molding can be difficult. Many times, in order to replace the molding, it may also be necessary to replace or reseal the glass. In short, PVC reveal moldings, relatively inexpensive parts, are very expensive to service. Outside of general assembly and processing issues, there are 5 variables that may cause a failure in the performance of a stationary glass reveal molding. They are as follows: material degradation, crystallization, plasticizer loss, material properties, and molded-in stress. Because of modern standard PVC formulations and the material requirements of most automotive companies, material degradation, crystallization and plasticizer loss do not commonly cause failure. Material properties and molded-in stress do.
Technical Paper

Evaluation of Finesse/Polish of Automotive Clearcoats

1998-02-23
980978
Minor surface defects in the clearcoat film are common place realities in modern automotive painting operations. Finessing and polishing processes are required to remove these defects and restore the clearcoat to its original condition. Evaluation of new clearcoat technologies and polishing processes has always been very subjective. This drove the development of a standardized test method for evaluating the finessability of a clearcoat. In this paper the authors will compare and contrast the differences between the traditional method used to evaluate finessability with the newly developed standardized method. The standardized method shows distinct advantages when evaluating different clearcoat technologies and polishing processes.
Technical Paper

1997 GM 5.7 LITER LS1 V8 ENGINE

1997-02-24
970915
General Motors Powertrain Group (GMPTG) has developed an all new small block V8 engine, designated LS1, for introduction into the 1997 Corvette. This engine was designed to meet both customer requirements and competitive challenges while also meeting the ever increasing legislated requirements of emissions and fuel economy. This 5.7L V8 provides increased power and torque while delivering higher fuel economy. In addition, improvements in both QRD and NVH characteristics were made while meeting packaging constraints and achieving significant mass reductions.
Technical Paper

1996 GM 7.4 Liter Engine Upgrade

1996-02-01
960012
General Motors Powertrain Division has developed the next generation big block V8 engine for introduction in the 1996 model year. In addition to meeting tighter emission and on-board diagnostic legislation, this engine evolved to meet both customer requirements and competitive challenges. Starting with the proven dependability of the time tested big block V8, goals were set to substantially increase the power, torque, fuel economy and overall pleaseability of GM's large load capacity gasoline engine. The need for this new engine to meet packaging requirements in many vehicle platforms, both truck and OEM, as well as a requirement for minimal additional heat rejection over the engine being replaced, placed additional constraints on the design.
Technical Paper

Nonlinear Analysis Theory of Single Leaf Steel Springs

1988-11-01
881744
The analytical methods for single leaf steel springs should at least include two areas: (1) allowance for any curved or tapered shape, and (2) technologies to precisely predict the geometrical configuration due to large deflection. The last item is an outstanding consideration in automotive application because of the parts alignment requirement. In this paper, a practical analytical method is presented to achieve the goals mentioned above. Basically, the. flexibility method of finite element was employed in the solution technique. In the spring application, this approach can save computer time because of the elimination of matrix inversion in the internal computation. An integration form of the flexibility matrix for each element was given in this paper to allow for a tapered spring shape. This integration-formed flexibility matrix can be approximately evaluated by the Gaussian Quadrature Formula.
Technical Paper

Driver Understanding and Recognition of Automotive ISO Symbols

1988-02-01
880056
This study assesses the understanding and recognition, by U.S. drivers, of the 25 automotive ISO symbols specified in SAE Standard J1048. A two-part survey was administered to 505 volunteers at a Secretary of State's office located in a Detroit suburb. Percentage results for symbol understanding indicated low levels of understanding for many symbols; percentage results for symbol recognition were generally much higher for all symbols. The effects of gender, age, and education level on the percentage results are summarized.
Technical Paper

Development and Validation of Engine Models Via Automated Dynamometer Tests

1979-02-01
790178
An automated engine dynamometer test procedure is developed and mathematical models for the main engine control variables are derived from the resulting data base. The new procedure involves sequential testing at many speed/load conditions for various combinations of air fuel ratio, spark timing and exhaust gas recirculation. The total testing time required for generating the data base of more than 2000 test points is less than twelve hours. An independent transient speed/load test is also conducted for the purpose of validating the engine models. The measured and model predicted data are compared for this test which corresponds to a segment of the EPA urban schedule.
Technical Paper

Emission and Fuel Economy Measurement Improvements

1979-02-01
790233
A program was initiated to improve the emission and fuel economy measurement accuracy and test cell to test cell correlation. Improvements were made to the Constant Volume Sampling System, electric dynamometer, instrument calibration ranges and system checks were initiated to improve the accuracy of the bag emissions, modal emissions, calculated and measured fuel economy. Unique emission and fuel economy problems associated with gasoline and diesel testing were studied and resolutions effected when possible.
Technical Paper

Changing Inspection and Maintenance Requirements: … A Result of New Emission Control Technology

1979-02-01
790783
Amendments to the Clean Air Act require the implementation of inspection/maintenance (I/M) programs in areas designated as non-attainment and unable to meet the National Ambient Air Quality Standards by 1982. Current I/M programs have been developed using data representative of pre- and early-catalyst emission control technology. Changes to current emission control systems and electronic computer controlled systems represent new emission control technology. This paper addresses the I/M situation as related to these system changes. Results of tests on a prototype system are presented. Parameter inspection and the utilization of built-in diagnostics on future systems have the potential to maximize the effectiveness of I/M programs.
Technical Paper

General Motors Phase II Catalyst System

1978-02-01
780205
Three-way catalysts provide a means of catalytically achieving lower NOx emission levels while maintaining good control of HC and CO emissions. However, very accurate control of air-fuel ratio is necessary. The precise air-fuel ratio control required is accomplished by employing a closed loop fuel metering system in conjunction with an exhaust gas sensor and an electronic control unit. To gain production experience with this type of system, General Motors is introducing it on two 1978 engine families sold in California. One is a 2.5 litre L-4 engine and the other is a 3.8 litre V-6 engine. Closed loop controlled carburetors are used on both systems. This paper discusses these 1978 systems. The components used on both systems are described and emission and fuel economy results are reviewed.
Technical Paper

Dual Catalytic Converters

1975-02-01
750176
The stringent 1978 emission standards of 0.41 gm/mi HC, 3.4 gm/mile CO, and 0.4 gm/mi NOx may require the use of a dual catalytic converter system (reducing and oxidizing catalyst). These emission requirements have been achieved at low mileage with such a system, but it is complex and has exhibited poor durability. This system also results in the loss of fuel economy at the 1978 emission levels.
Technical Paper

GENERAL MOTORS EXPERIMENTAL SAFETY VEHICLE-POWERTRAIN & FUEL SYSTEM

1973-02-01
730280
The Experimental Safety Vehicle powertrain and fuel system developed by General Motors in compliance with Contract DOT-OS-00095 with the U.S. Department of Transportation include several special features: a low engine accessory package to meet the front visibility down angle of 8 degrees, engine and transmission mounting for retention at high decelerations, a light aluminum engine, an over-the-rear-axle fuel tank, and a unique evaporative emission fuel pipe routing. A comprehensive test program was planned and final testing to validate contract specifications was conducted.
Technical Paper

DEVELOPMENT OF THE BRAKE SYSTEM FOR THE GENERAL MOTORS EXPERIMENTAL SAFETY VEHICLE

1973-02-01
730081
The Experimental Safety Vehicle program in General Motors was a study in meeting the Department of Transportation performance requirements, with the sole objective being to meet or exceed all of the contract specifications. This vehicle was not intended for production; it was a safety idea car with many unique features including a four-wheel, anti-lock disc brake system using a hydraulic power brake system with an electro-hydraulic back-up system. In addition, the design of the dual piston caliper for the disc brakes provides a redundant system thereby minimizing the effect of a single line or hose failure. This feature coupled with the redundant back-up power brake system provided performance under various failed conditions approximately equal to the original effectiveness with only a slight increase in pedal effort. This brake system, developed for the ESV, satisfied the General Motors performance objectives, and equaled or surpassed the contract requirements of the ESV program.
X